The Solutions
The campus heating and energy system underwent a comprehensive overhaul to address inefficiencies, safety risks, and rising operational costs associated with the aging steam plant. Prior to the upgrade, the 18 buildings served by the centralized steam system faced substantial energy losses and safety challenges due to widespread steam leaks, failing condensate return pumps, and exposed steam piping. The deteriorating infrastructure forced the steam boilers to operate at an elevated base load year-round, as they also provided domestic hot water for residence halls, resulting in a high gas Energy Use Index (EUI) of 61.85 kBTU/ft²/yr. Maintenance issues were further exacerbated by the limited availability of replacement parts for aging equipment. A critical failure of the system during winter, which affected space heating and domestic hot water in several residence halls, highlighted the urgent need for modernization.
In place of this system, CMTA introduced localized heating through the installation of 12 gas-fired condensing boilers and 12 gas-fired condensing domestic water heaters across 14 buildings. By decoupling the heating hot water and domestic hot water systems, the university achieved significant operational efficiencies, particularly during the cooling season, as boilers could now operate with a 15:1 turndown ratio. This flexibility ensured the system could respond more efficiently to actual building load demands, reducing energy waste. Following the upgrade, gas EUI dropped to 29.25 kBTU/ft²/yr, representing a substantial improvement in energy performance.
However, to implement this system, CMTA had to overcome complex logistical and environmental challenges with creative and efficient solutions. One of the most significant challenges was installing 3,700 linear feet of underground EPDM natural gas piping without disrupting the 24/7/365 campus operations. To avoid safety risks, preserve ADA access, and minimize noise pollution, the team employed horizontal boring techniques rather than traditional trenching methods. This innovative approach allowed piping lines to be run beneath existing utilities such as internet, water, and electricity without impacting critical infrastructure or incurring repair costs.
Alongside the heating system retrofit, a series of Energy Conservation Measures (ECMs) were implemented to improve overall electrical efficiency. These included replacing 19 air handling units, 2 rooftop units, and 1 kitchen makeup air unit, as well as recommissioning a previously inactive solar array and completing a campus-wide LED lighting retrofit. The project also involved a full Building Automation System (BAS) recommissioning, integrating advanced controls such as outside air system lockouts, outside air setpoint resets, and variable speed operations with the addition of VFDs. Post-upgrade, the campus-wide electrical EUI decreased from 42.8 kBTU/ft²/yr to 38.69 kBTU/ft²/yr, demonstrating measurable sustainability gains.